New Reefing System

There was no reefing system installed. The mainsail has two reef points with grommets to tie, but no mechanism to backhaul or shape the reefed sail. The problem was addressed by adding two cheek blocks, and to cleats to the starboard side of the boom and two pad eyes to the port. Reefing lines were the run from pad yes, under the sail pack, through the reef clew, back down under the sail pack, through the block and to the cleat. The blocks and cleats were offset to avoid interfering with one another. The cleats were placed near the main halyard so they can be operated from the same position.

Staysail and Mainsail Halyards Shortened

The halyards are cable spliced onto rope. The cables of the staysail and mainsail halyards were too long to allow the sails to be raised completely because the winches were not designed for wire. Today I shorted each by a couple of feet (as I did previously for the jib halyard), so all the sails are operational.

The Vessel Was Formally “Denamed”

In keeping with traditions, our vessel was formally “denamed” today (in preparation for the renaming ceremony). Once every reference to the old name had been removed , we prepare an “ingot” with the old name and invoked the name of the ruler of the deep as follows:

“Oh mighty and great ruler of the seas and oceans, to whom all ships and we who venture upon your vast domain are required to pay homage, implore you in your graciousness to expunge for all time from your records and recollection the name “Stormy” which has ceased to be an entity in your kingdom. As proof thereof, we submit this ingot bearing her name to be corrupted through your powers and forever be purged from the sea.”

First Time Out of the Slip

The boat was finally ready for a test run to learn more about the leak in the engine’s coolant system. We motored just outside the Bahia, tested the instruments, raised the sails, and when motoring back took some time to practice motoring skills using a mooring buoy.

Notably, we learned the boat speed was not being reported, the halyard for the mainsail needs to have its cable shortened, and the coolant leak is substantial, perhaps leaking a quart. The problem with the halyard prevented us from sailing, which was a moot point as there was no wind (one of the reasons we chose the day to go out). We also discovered the prop walk forces the bow to the starboard when backing out of the slip (will need to figure out a way to control that) and it is almost impossible to turn the stern to the starboard while in reverse.

Sail Pack and Lazy Jack Installed

We completed a Sailrite Sail Pack Kit.this is the largest project we have sewed date. Fortunately, the roof of the rental was large enough to stage the project.

Having a portable sewing machine was particularly helpful during the final stages of completing the project, for example, sewing the batten pockets closed.

The sail pack was installed and held up with a lazy jack system.

The sail pack was constructed according to the directions provided by Sailrite with the exception that the PVC battens were replaced with fiberglass tubes. The challenge in using fiberglass is shipping, This problem was overcome by using the Max-Gain System (MGS). The MDS 3/4″ round tubing is 93″ long and has an i.d. of 1/2″. The tubing is connected using solid 1/2″ fiberglass rod using J-B Weld.

The lazy jack was purchased from Nautos and comprises of blocks and 12-strand polyester rope. After installing the system, we decided it will likely be temporary, and it will eventually be replaced with low-friction rings and Dyneema. After using/tuning the existing lazy jack system for awhile, it will be disassembled and used as a template for the Dyneema system.