Cabinet Constructed for New Stove

The original stove was probably a two-burner propane model. During the refit in the early 2000’s, a genset was installed, the propane stove and locker were removed, and a non-gimbaled induction cook surface and convection oven were installed. Toward our goal of being environmentally friendly, we removed the diesel-burning genset and the galley appliances. Our options for a replacement propane stove were limited. In fact, there was only one commercial stove that would fit, a Force 10 “Euro Sub-compact” 3-burner stove. Unfortunately, the new stove is about 3 inches narrower than the previous one. As a first effort, we made a spacer out of teak (using the discarded cheeks from the rudder). While functional, we did not like the appearance., the gap seemed to invite dropping things in the crevasse, and it did not seem sturdy enough. So, we set out to construct a proper cabinet. Because the brackets for the new stove required high tolerance (within a 1/4″ in width) and the existing cabinet was (naturally) not square, it was necessary to have proper woodworking tools. Unfortunately, ours were not in Mexico. We borrowed a cheap miter saw from a relative in Tucson and purchased an inexpensive table saw from Home Depot. As an aside, we highly recommend the Ryobi RTS12T Table Saw for about $200. While at Home Depot in Tucson, we also picked up some 1 x 3″ (actually 0.75 x 2.5″) appearance board. To make the construction easier, we also picked up a cheap nail gun at Harbor Freight (on sale for $20) and used the compressed air in the yard. The first step was to create a frame (the piece in the back is temporary and some of the components required gluing before ripping to the proper width).

After filling the nail holes, sanding, varnishing (necessary to apply the veneer), and sanding smooth, we insulated with some fiberglass and installed locally-sourced 20 gauge 306 stainless.

Teak veneer with 3M self-adhesive is easy to cut (and trim once applied) with a sharp utility knife, and once a couple of coats of varnish are applied, it is unlikely to come off.

Because considerable effort was put into “measuring ten times and cutting once”, the stove fit like a glove.

A bonus of the stainless firewall is the lock for the gimbal (lower right) is simply a hole drilled in the firewall (no need to install the hardware supplied by Force 10). As a note, if you are going to drill through stainless, you will need cobalt-tipped bits.

Rudder Has Been Rebuilt

The original problem in the rudder was delamination, which we detected during the original survey by “tapping” the fiberglass. After drilling a hole to check the integrity of the foam (which was fine) and establish the core was dry, the delaminated section was cut out.

After the edges of the cutout were ground beveled, the area was built up again with a series of increasingly larger pieces of mat. A small section of the rudder at the position of the middle gudgeon was removed (shown in lower right) to allow the rudder to be more easily removed without the need to remove the corresponding pintle.

Stress fractures were ground out and patched.

The entire rudder was covered with a layer of mat.

The backside of the new 316 stainless-reinforced cheeks (April 22 post) were glassed, then they were mounded to the rudder with countersunk 316 stainless bolts.

A spacer was fabricated from the old teak cheeks and the bolt holes were filled with epoxy.

The entire rudder was covered in mat and epoxy mixed with West Systems 407 filler (which makes it easier to sand).

After sanding, the entire rudder was coated with epoxy mixed with some primer. Below the waterline, the epoxy was mixed with a powdered aluminum vapor barrier (the darker color).

After several months of work, the rudder is now ready to be remounted on the boat.

The Rudder Has Been Removed

The twelve bronze bolts were removed from the rudder using an impact hammer. They came off with surprising ease considering they have been underwater for the better part of five decades. Once unbolted, it was possible to chip away at the gel coat that encapsulated part of the bronze gudgeons.

The pintles were left mounted to the hull, which made it more difficult to remove the rudder, However, with the help of a crane and after removing the wind vane, there was just enough room to move the 300 lb rudder straight back and clear the gudgeons. Alejandro, shown in the photo, has been hired to repair the rudder, which has some separation and also needs the cheeks attached and fiberglassed over.

Replacement Cheeks Fabricated for Rudder

The original teak cheeks for the rudder experience dry rot and the previous owner cut the tops of them and fabricated a very ugly stainless steel can to replace them. However, this changed the lines of the boat dramatically. It is not possible to obtain high-density teak anymore and low-density teak does not have the same structural strength. In fact, even the original teak cheeks experience cracks where the bolt for the tiller passed, and that point was definitely the weak link in the design. So, we fabricated new cheeks using the original shape using marine plywood. The original cheeks were 1-1/2″ thick, so we employed two layers of 3/4″ plywood and to afford even greater strength for the stress of the tiller we sandwiched in-between the layers of plywood a sheet of 3/16″ stainless. The stainless was cut to shape with an angle grinder, drilled with cobalt-tipped bits, and the plywood was routed out to accommodate the piece of stainless steel.

The two halves of plywood were glued with epoxy, the edge was rounded with the router, and the cheeks were soaked in resin.

The cheeks will be mounted to the rudder with countersunk bolts (just like the original teak cheeks), but the bolt holes will be filled with resin and the cheeks will be covered with layers of fiberglass, thereby creating a sold fiberglass rudder that will be considerably stronger than the original. we will fabricated a spacer for the top of the cheeks out of the original teak cheeks.

Brightwork has Been Refinished

All the teak on the deck has been taken down to bare wood (using a head gun and scraper), screw hols were plugged with dowels, cracks were filled with epoxy and sawdust, and ten coats of Man-O-War glossy varnish has been applied. Once we splash the boat (and are away from the dust of the work yard) we will sand the brightwork and apply a couple more coats of varnish.

Rebuilding the Barient Winches

The Aegir-Ran has eight Barient winches. Developed more than half a century ago, Barients were the first two-speed winches geared in both directions. At some point Lewmar bought Barient and most parts for the winches are no longer available. Our winches had not been serviced in some time and the primary 28 STS winches in particular were stiff and practically unusable. Winches are expensive and replacing the primaries would cost about $5000 a pop. so we set out to rebuild them. Unfortunately, the 28s were poorly designed with a bronze gear housing mounted on an aluminum base with stainless steel bolts. Electrolysis had practically fused the aluminum to the bronze. To make removing of the 28s for servicing even more complicated were six eight-inch bolts that passed through the hull. The bolts had been gooped in so it was impossible to simply unbolt the winches to remove them for servicing. The order of removal had to be the drum, followed by the gear housing, followed by the base. While it proved possible to disassemble the port 28 without much difficulty, it was clear that the 28 on the starboard side was in much poorer shape. While the drum could be removed, the four bolts that held the gear housing to the base were frozen. After soaking in Liquid Wrench for a day, only two of the bolts could be removed with a wrench. Eventually, two of the Allen bolt heads were stripped.

After three days of effort, the stripped bolts were eventually removed with an extractor using an impact winch.

After a day’s work, separating the housing from the base was eventually achieved by using a Dremel tool and a cutting wheel to create separation and a rubber mallet. The dirt in the base evidenced the winch had not been disassembled or properly maintenanced for decades.

Eventually, all five of the cockpit winches were removed and an assembly line was created to disassemble and clean the parts.

Using the aluminum foil and vinegar trick, it proved possible to polish the chrome to like-new condition.

Luckily, a pair of non-self-tailing Barient 28s were found on eBay that had STAINLESS STEEL bases.

After about nine days of work, the winches were reassembled and now operate like new.